This thread relates to my ACU-200 that incorrectly responds when operated in "Track" mode. When the autopilot was set to "Track" mode to navigate towards a selected waypoint that was approximately 10 nm fro current position, the autopilot steered the vessel 180 degrees from the destination waypoint, traveled approximately 0.25 nm, and signaled waypoint arrival. A second that third attempt yielded the same result.
It should be noted this autopilot performs perfectly when operated in "Auto" mode, but has not been tested in any pattern modes.
It should be noted this autopilot performs perfectly when operated in "Auto" mode, but has not been tested in any pattern modes.